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OEM’s Vendor Development Project




         Final Presentation

Electropolymers Pvt. Ltd.
             17th July 2012



  SMEDA-JICA Industry Support Program
Name                    Designation
Shaheer Hassan          Assistant Manager, Quality
Faizan Arshad           Executive Quality Assurance
Saleem Sharif           Production Supervisor
Adnan Islam.            Manager Quality Control.


       Members from SMEDA-JICA
Kiyoshi Yoshida                       JICA Expert
Syed Babar Umar                  SMEDA Counter Part
Muhammad Naeem Ansari            SMEDA Counter Part


  Total number of Visits: 11      Evaluation Date: 25th May.

                 Duration of Activity: 2 months.
   Introduction of Company.
     Company Mission and Vision.
     Main Products.
     Client Area.
     Organogram.
   Electropolymers and SMEDA.
   Product Selection for Working (Rear Combination) and Reasons for
    selection.
           Supply and forecast Graph.
       Productivity Improvement.
             Status before improvement.
             Target setting.
             Problem defining.
             Old Layout of Assembly line.
             Cycle time study.
             Takt Time study.
             Line Balancing graph with Efficiency.
             ECRS Implementation.
   Line Balance graph with Efficiency after Improvements.
             New Layout of Assembly line after Improvements.
             Results of Improvements (Summary).
             Work Content Analysis Chart.
       Quality Improvement.
           Suggestions from SMEDA and JICA expert.
           KAIZEN
             Implemented KAIZEN.
             Un Implemented KAIZEN.
           Summary of KAIZEN.
           Cost Savings by KAIZEN.
           FINAL RESULTS.

   Product Selection for Working (Cultus).
           New Line Layout and Proposal.
             Takt time and Work content Analysis.
             Proposal of new line from JICA/ SMEDA.
             Future Plans.
Welcome At Electropolymers Pvt. Ltd.
In a world where quality increasingly touches
every aspect of our daily lives, we will be
leading quality provider in the automotive
lamp manufacturing industry to become the
most admired company in our industry as seen
by our OEMS.
Our mission is to retain our position as a leading
Pakistani manufacturer of automotive lamps, our
prime priority will be ZERO DEFECT supplies
backed by responsive service and empowered
employees. The quality of products further been
upgraded and our thrust is to achieve optimum
level.
Atlas Honda
Honda Atlas Car Pakistan Limited
Suzuki Motor Cycle
Pak Suzuki Motor Company Limited
Dawood Yamaha Limited
Millat Tractors Limited
Dewan Farooque Limited
To synchronize the processes.
To Increase the productivity
To reduce system wastages
To improve product quality & reduce the rejections.
To seek guidance from program regarding layout for
  new products.
1. Rear Combination Lamp SB-308

 Areas of Intervention:
  a) Productivity Improvement
  b) Quality Improvement

2. New Lamps Layout
SB-308 Rear Combination Lamp
   Because of the High Lead Time.
 Because of the large number of manpower engaged.

 Because of High wastage.

 Since the volume of Rear combination is increasing,

a consistency was required in the production for meeting
the schedule dates.
Screw




                                        Lens
Reflector




                     Rear Combination




            Gasket                         Bulb & Harness
MODEL / (Selected Product)       Rear Combination
Current Production Volume:       3600
NO. Of Operators:                8
Bottleneck Process Cycle Time:   149.9
Production Lot Size:             200 sets
Transportation Lot Size:         10 pieces /carton
Processing Time:                 612.4 sec
No. Of Deliveries / Month        4
Total Working Hours:             184 hrs/month
Overtime                         0
Productivity                     100%
Line Balancing Efficiency        51%
Cost reduction by 30%.
Reduction of Work space by 30-40%
Processing time reduction by 30-40%.
Wastage reduction by 70-80%.
High Process time. (612.4 sec)
Excessive workers (8 workers engaged)
Process redundancy. (Non Value added
   processes)
Wastages. (Wastage of Time, Material, Man hours
   and Material)
Efficiency was around 51%
Before KAIZEN


                                                          5




                         2           3            4



                                                      6

                              8              7
    1




8 workers were involved in the production of Rear Combination Light.
   Tact time is the exact time required to process
    one product

       Tact Time =       Monthly Operating Time
                         Monthly Production Quantity


        Old Takt time=    184/3600           hours/piece
        Old Takt time=    (184/3600)x3600= 184 sec/piece


        New Takt time=   184/5108           hours/piece
        New Takt time=   (184/5108)x3600= 130 sec/piece
The graph is showing the Adhesive
                                                                       cleaning as a bottleneck process.

                                                                       The Idle time was very high for
                                                                       several processes for example Idle
                                                                       time for Taping process was up to
                                                                       89.33%.

                                                                       The efficiency of the processes
                                                                       was 51%.
                            sum of working hours of each process
Balance Efficiency   =                                                          x100

                            maximum time of process x the number of processes




                     =51%
ECRS study was carried out in order to reduce the non
value added processes and to eliminate the redundancy.
                 E- Eliminate
                 C-Combine
                 R-Re arrange
                 S-Simplify
Previously a non value added process
Taping was followed which had no
impact on the Product.



                                                   Taping
                                                   applied




                                       The taping was done to prevent the
                                       flowing of adhesive from the back of
                                       reflector. After bonding, It was
                                       removed.
Bulbs were verified at Final Inspection
after complete assembly. The process
is now eliminated and the bulbs are
verified at the time of fitment.




                                             Bulb
                                          verification
Previously two different workers were
performing the processes of
Inspection and Packing.




The packing of parts is done by the
inspector at Final Check point.
Previously two different workers were
                            performing the operations of Bulb,
                            harness and screw fitment.




The processes of Bulb, harness and
screw fitment are now combined in a
single process.
The process of Taping was removed by
Gasket fitment. Formerly, taping was
applied which was then removed
having no impact on the product.




                                       The processes are now re arranged by
                                       putting the process of Gasket fitment
                                       at the first place instead of taping.
The testing unit is now simplified and
                                       is made common for both the lights.




Previously the testing unit for Rear
combination had two different units
for Left and Right hand lights.
Previously the worker had to put the
                          light in press fitment and then had to
                          locate the upper jig.



                            Upper part

                            Lower part



Now a jig is developed for Press
fitment.




                New Jig
   Screw gun was previously placed
                                 on the table and hence every time
                                 the worker had to take the gun
                                 and fit the screws.




   The Screw gun is hanged near the
    screw fitment and hence the
    worker is facilitated.
   The Gasket fitment process is
    eased by making a jig for
    applying adhesive on the Gasket   1
    and pasting the Gasket on the
    Reflector.




       2
sum of working hours of each process
                             sum of w orking hours of each proces s                       Balance Effici ency
Balance Effici ency                                                                                             =                                                           x100
                      =                                                            x100
                                                                                                                     maximum t ime of process x t he number of proc esses
                             maximum t ime of process x the number of proc esses




                      =51%
                                                                                                                =85.87%
After
            KAIZEN
    2   3                 4
                                  5
                      6
    1
                 Before
                KAIZEN
                                                  5
            2                 3           4
                                              6
                  8                   7
1
Improvement
       Parameters              Before          After
                                                                  %

                                                                  22.6%
     Total Cycle Time         612.4 sec      474 sec
                                                               reduction
                                                                 34.87%
 Line Balance efficiency         51%          85.87%
                                                                increase
     No. of Workers               8               6          25% reduction

Cost reduction in terms of 81.6 min/total   47.4 min/total       41.9%
                                               workers
      workers’ time           workers                          reduction

       Space saving            264 ft²        216ft²         18.2% saving
Work Content analysis was done for two different
processes in Leakage testing.
2)1) Leakage testing without Air
3)2) Leakage testing with Air.
The reflector was cut in order to see the gap between the Lens
and the Reflector.
The Lens has a window which is shown in the picture.
It was recommended to make a inner wall in the Lens to avoid
Leakage
The time of Press fitment was
                      changed from 45 seconds to 6
                      seconds in order to ensure that the
                      locks are properly seated.




Previous
  time

           New time
The flashes inside the channel along
the leaked area were removed and
then adhesive was applied.




                                 The purpose was to check whether the
                                 flashes were the root cause for
                                 leakage or not.
After Press fitment, the pieces are
placed upside down on the table to
ensure proper adhesion of Lens
and Reflector.




                      The purpose was to retain the adhesive along
                      the channel and impart a pressure so as to
                      confirm the proper adhesion.
Process: Sealing                   Team:                     Leader:                             Suggest: SMEDA-JICA
Before (Problem)
         1. Possible damage of Hot Melt Nozzle
              Because it was installed on the               After (Improvement)
                       passage

           2. Possible part defect caused by
                                                         Move the Hot Melt Nozzle to inside the process
                        collision
                      (other worker)




  Date             Target (round mark)                Status (round mark)         Productivity Result
                                                                                      [Before – After (sec/pcs)] x Production Vol.
    2012-5-29                                                  Done
                                 Productivity                                                           (pcs/mth)
                                                           Progressing
                            Quality, Cost,    5S,             Future
  NO.                 Safety, Other_PM (machine protect)       Reject                    Reduced time :       0     hrs./month
            1
Mr. Salim / Mr.
Process: Pressing                    Team:                Leader:                       Suggest:             Adnan
 Before (Problem)                                  After (Improvement)
                                                          Change the upper and lower die and upper
 It takes long time to use the press machine.
                                                         die fix to the moving plate so that worker can
                                                                              use
1. The worker has to hold the upper base plate
                                                         Both hands for loading and unloading of the
 in one hand and put the part from second hand.
                                                                             parts.
2. Possibility of damaging the part and also it
     take long time to perform the operation.
                                                                    *Shorten the operation time.
                                                                     *Makes worker task easier.




 Date               Target (round mark)            Status (round mark)    Productivity Result
                                                            Done              [Before – After (sec/pcs)] x Production Vol.
   2012-6-5                                                                                     (pcs/mth)
                              Productivity              Progressing
                                                                                (37-20)sec/pcs x 3600pcs/month= 61200
                        Quality,   Cost,   5S,             Future                              sec/month
 NO.                Safety, Other(_____________)            Reject
         2                                                                    Reduced time : 17               hrs./month
Process:                            Team:                   Leader:                           Suggest: Mr. Salim
Before (Problem)                                         After (Improvement)

       Sealing performed after application of                 Rearrange the process and eliminate
            masking tape on every part                             “Waste of process itself”
      *Take much time to masking & remove it                  *Eliminate Waste process (application of
            “Waste of process itself”                                      masking tap)
                                                                       *Reduce working time
               *Waste of masking tape                        *No masking tape required (cost reduction)

                                                              Before
                                                         1.Sealing                                After
                                                                                          1.Gasket fitment
                                                         2.Bonding/Press                  2.Bonding/Press
                                                         fitment                          fitment
Masking
                                                         3.Adhesive cleaning              3.Adhesive cleaning
 tape
                                                           Remove Tape                    4.Leakage test
                                                         4.Leakage test                   5.Screw/ Bulb &
                                                         5.Tightening                     Harness
                                                         6.Gasket fitment                   fitment
                                                         7.Assemble harness               6.Final testing +
                                                         8.Final testing                  Packing
                                                         9.Packing

Date               Target (round mark)               Status (round mark)       Productivity Result
                                                                                   [Before – After (sec/pcs)] x Production Vol.
  2012-6-5                                                    Done
                                Productivity                                                         (pcs/mth)
                                                          Progressing
NO.                       Quality,   Cost,   5S,             Future               (16-0)sec/pcs x 3600pcs/month= 57600sec/month

           3       Safety, Other(____Space_________)          Reject                 Reduced time : 16            hrs./month
Process: Leakage Testing             Team:                 Leader:                          Suggest: Mr. Salim
 Before (Problem)
                                                     After (Improvement)
        1.It takes long time to check the leakage                    Use low pressure air for check.
           2. Possible overlook the water leak                              Check by bubble

       Dip into water and check if water goes into                  *Shorten the checking time.
                         the part                                *Ensure the leakage inspection.
                                                         *No water goes into the part (therefore shorten the
                                                                           cleaning time)




                                                                                              Low Pressure Air


 Date               Target (round mark)              Status (round mark)     Productivity Result
                                                                                 [Before – After (sec/pcs)] x Production Vol.
   2012-6-10                                                  Done
                              Productivity                                                         (pcs/mth)
                                                          Progressing
                        Quality,   Cost,   5S,               Future
 NO.                Safety, Other(_____________)
           4                                                  Reject            Reduced time :                     hrs./month
Leader:                       Suggest:      SMEDA-JICA
Process: Gasket Fitment              Team:

 Before (Problem)                                    After (Improvement)

  1-It took long time to perform the operation       1. The idea is to develop a jig with embossed same
 Because the glue stick with the workers hand        Profile as of gasket and it has little higher with base
   and also the gasket stick with card board.                                so that
    2. Make Operator task more difficult.                        Glue does not stick with base.
                                                     2. There will also be location pins as there are holes
                                                                     Available in the gasket.

                                                      It will make the operator work more easy and lesser
                                                                         time is required.
                                                     Location Pins




                                                           Jig base




 Date               Target (round mark)            Status (round mark)     Productivity Result
                                                                               [Before – After (sec/pcs)] x Production Vol.
   2012-5-29                                                Done
                              Productivity                                                       (pcs/mth)
                                                        Progressing           (100.57-79)sec/pcs x 3600pcs/month= 77652 sec/
                        Quality,   Cost,   5S,             Future                                  month
 NO.
         5          Safety, Other(_____________)            Reject              Reduced time : 21.57          hrs./month
Team:               Leader:                                      SMEDA-JICA
Process: Final Testing                                                                 Suggest:
Before (Problem)
                                                  After (Improvement)

     There was no proper place for                       A holder is attached to save the
      putting the markers used in                                      time.
    marking the parts and there fore
   the worker took time in marking.




Date               Target (round mark)            Status (round mark)   Productivity Result
                                                                            [Before – After (sec/pcs)] x Production Vol.
  2012-6-10                                                Done
                             Productivity                                                     (pcs/mth)
                                                       Progressing
                       Quality,   Cost,   5S,             Future
NO.                Safety, Other(_____________)
        6                                                  Reject       Reduced time :           0           hrs./month
Team:               Leader:                                     SMEDA-JICA
Process: Final Testing                                                                 Suggest:
Before (Problem)
                                                  After (Improvement)


                                                        Coupler was fixed in the Jig which was
                                                               previously not attached




Date               Target (round mark)            Status (round mark)   Productivity Result
                                                                            [Before – After (sec/pcs)] x Production Vol.
  2012-6-10                                                Done
                             Productivity                                                     (pcs/mth)
                                                       Progressing
                       Quality,   Cost,   5S,             Future
NO.                Safety, Other(_____________)
        7                                                  Reject        Reduced time :         0             hrs./month
NO.
  OF
IDEAS    BEFORE   AFTER                    TARGET OF
 Total   SMEDA    SMEDA   IMPLEMENTED   IMPLEMENTATION     Time saved



                                                               88.2
 12        0       12          7        1 week of August
                                         st
                                                           hours/month
Process:                           Team:                 Leader:                      Suggest:

Before (Problem)                                   After (Improvement)

       Excessive length of bolts

  *It take long time to tighten nuts




Date                                              Status (round mark)    Productivity Result
                   Target (round mark)
       2012-5-29                                                          [Before – After (sec/pcs)] x Production Vol.
                             Productivity                Done                               (pcs/mth)
NO.                    Quality,   Cost,   5S,         Progressing
            0      Safety, Other(_____________)         Future           Reduced time :                     hrs./month
                                                        Reject
Process:                           Team:               Leader:                              Suggest:

  Before (Problem)                                    After (Improvement)




Date                                                                        Productivity Result
                   Target (round mark)            Status (round mark)          [Before – After (sec/pcs)] x Production Vol.
       2012-5-29                                                                                 (pcs/mth)
                             Productivity               Done
                       Quality,   Cost,   5S,        Progressing
NO.
            0      Safety, Other(_____________)        Future                Reduced time :                      hrs./month
                                                       Reject
Process:                        Team:                 Leader:                         Suggest:

Before (Problem)                                   After (Improvement)



                                                        Example of
       Inadequate lightening for Test               lightening at Auto
                                                      Assembly Line
       *Possible overlook the defects

                                                       Dedicate
                                                  Lightening for Test




                                                                         Productivity Result
Date                                               Status (round mark)        [Before – After (sec/pcs)] x Production Vol.
                      Target (round mark)
       2012-5-29                                                                                (pcs/mth)
                             Productivity               Done
NO                     Quality,    Cost,  5S,        Progressing
 .                 Safety, Other(_____________)        Future             Reduced time :                     hrs./month
             0                                         Reject
Process:                               Team:              Leader:                           Suggest:

    Before (Problem)                                    After (Improvement)


 This worker is just holding Jig (waste of time)                   Hold the Jig by Clamp or something



Unload lamps one by one (take a long time)                    Remove the springs one side all then after
                                                               remove the other side of spring so that
                                                                 unloading time will be shortened
                     Picture or figure




Date                                               Status (round mark)        Productivity Result
                    Target (round mark)                                          [Before – After (sec/pcs)] x Production Vol.
       2012-5-29                                                                                   (pcs/mth)
                             Productivity                  Done
 NO.                   Quality,   Cost,   5S,           Progressing
                   Safety, Other(_____________)           Future               Reduced time :                      hrs./month
        0                                                 Reject
Leader:                       Suggest:      SMEDA-JICA
Process:                            Team:
Before (Problem)
                                                    After (Improvement)

   Material handling should be improved by
   making the trolleys in order to reduce the
   risk of damaging.




Date               Target (round mark)            Status (round mark)     Productivity Result
                                                                              [Before – After (sec/pcs)] x Production Vol.
   2012-5-29                                               Done
                             Productivity                                                       (pcs/mth)
                                                       Progressing
                       Quality,   Cost,   5S,             Future
NO.
           5       Safety, Other(_____________)            Reject            Reduced time :                     hrs./month
Time saving on Rear comb. Line                    =(41.9/100)x184
Time saving on Rear comb. Line                    =77.096 Hrs/month
Time saving on Rear comb. Line
                                                 =925.152 Hrs/year

Cost saving on Rear comb. Line by saving time     =77.096x43.47

Cost saving on Rear comb. Line by saving time     =3352 Rs./month

Cost saving on Rear comb. Line by saving time     =40224 Rs./year

Cost saving by worker reduction                  =2x8000

Cost saving by worker reduction                  =16000 Rs/ month.

Cost saving by worker reduction                 =192000 Rs/ year.


Total saving                                    = 1,92,000+40,224 Rs./year
Total saving per year
                                                = 2,32,224 Rs./year
Improvement     Improvement in
Description Before                   Target              Achieved           in %            Times
                                     Reduce to
Total Cycle Time    612.4 sec                              474 sec                        1.29
                                       1/3                                22.6%
  Line Balance
    efficiency          51%          Around 80%            85.87%         34.87%          1.68
 No. of Workers           8               4-5                  6          25% reduction   1.33
Cost reduction in
terms of workers’   81.6 min/total   min/total workers
                                                         47.4 min/total
      time
                       workers                              workers       41.9 %          1.72
  Space saving        264 ft²               -              216ft²         18.18%          1.22
                                                          2,32,224
                          0                 -                                      -             -
  Total Saving                                            Rs./year
    Y9f Cultus Head Lamp.

   Takt time and Work Content Analysis of Y9f Cultus Head Lamp.


                     Y9f Cultus Tail Lamp.


   Takt time and Work Content Analysis of Y9f Cultus Tail Lamp.
Control P.
                                                     Adh.
                                                   Applicator
                                                    0.85 x 0.5
                          CNC Spot Gluing
                           Machine 3 Axis
                              2.1 x 1.27


                                                      Press
Table-1                                              1.0 x 0.7




                                                                                        4.0 m
0.75 x 0.9




                                                                 0.75 x 0.9
                                                                          Table-2
                                                                 0.75 x 0.9
                                                                              Table-3
             Table-4
             0.75 x 0.9         Light Tester       Leak Tester
                                    0.9 x 0.85       0.9 x 0.7




                                           3.6 m
Implementation of KAIZEN.
Time study on other Assembly lines.
Final Presentation for SMEDA-JICA

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Final Presentation for SMEDA-JICA

  • 1. OEM’s Vendor Development Project Final Presentation Electropolymers Pvt. Ltd. 17th July 2012 SMEDA-JICA Industry Support Program
  • 2. Name Designation Shaheer Hassan Assistant Manager, Quality Faizan Arshad Executive Quality Assurance Saleem Sharif Production Supervisor Adnan Islam. Manager Quality Control. Members from SMEDA-JICA Kiyoshi Yoshida JICA Expert Syed Babar Umar SMEDA Counter Part Muhammad Naeem Ansari SMEDA Counter Part Total number of Visits: 11 Evaluation Date: 25th May. Duration of Activity: 2 months.
  • 3. Introduction of Company.  Company Mission and Vision.  Main Products.  Client Area.  Organogram.  Electropolymers and SMEDA.  Product Selection for Working (Rear Combination) and Reasons for selection.  Supply and forecast Graph.  Productivity Improvement.  Status before improvement.  Target setting.  Problem defining.  Old Layout of Assembly line.  Cycle time study.  Takt Time study.  Line Balancing graph with Efficiency.  ECRS Implementation.
  • 4. Line Balance graph with Efficiency after Improvements.  New Layout of Assembly line after Improvements.  Results of Improvements (Summary).  Work Content Analysis Chart.  Quality Improvement.  Suggestions from SMEDA and JICA expert.  KAIZEN  Implemented KAIZEN.  Un Implemented KAIZEN.  Summary of KAIZEN.  Cost Savings by KAIZEN.  FINAL RESULTS.  Product Selection for Working (Cultus).  New Line Layout and Proposal.  Takt time and Work content Analysis.  Proposal of new line from JICA/ SMEDA.  Future Plans.
  • 6. In a world where quality increasingly touches every aspect of our daily lives, we will be leading quality provider in the automotive lamp manufacturing industry to become the most admired company in our industry as seen by our OEMS.
  • 7. Our mission is to retain our position as a leading Pakistani manufacturer of automotive lamps, our prime priority will be ZERO DEFECT supplies backed by responsive service and empowered employees. The quality of products further been upgraded and our thrust is to achieve optimum level.
  • 8.
  • 9.
  • 10. Atlas Honda Honda Atlas Car Pakistan Limited Suzuki Motor Cycle Pak Suzuki Motor Company Limited Dawood Yamaha Limited Millat Tractors Limited Dewan Farooque Limited
  • 11.
  • 12. To synchronize the processes. To Increase the productivity To reduce system wastages To improve product quality & reduce the rejections. To seek guidance from program regarding layout for new products.
  • 13. 1. Rear Combination Lamp SB-308 Areas of Intervention: a) Productivity Improvement b) Quality Improvement 2. New Lamps Layout
  • 14. SB-308 Rear Combination Lamp  Because of the High Lead Time.  Because of the large number of manpower engaged.  Because of High wastage.  Since the volume of Rear combination is increasing, a consistency was required in the production for meeting the schedule dates.
  • 15. Screw Lens Reflector Rear Combination Gasket Bulb & Harness
  • 16.
  • 17.
  • 18. MODEL / (Selected Product) Rear Combination Current Production Volume: 3600 NO. Of Operators: 8 Bottleneck Process Cycle Time: 149.9 Production Lot Size: 200 sets Transportation Lot Size: 10 pieces /carton Processing Time: 612.4 sec No. Of Deliveries / Month 4 Total Working Hours: 184 hrs/month Overtime 0 Productivity 100% Line Balancing Efficiency 51%
  • 19. Cost reduction by 30%. Reduction of Work space by 30-40% Processing time reduction by 30-40%. Wastage reduction by 70-80%.
  • 20. High Process time. (612.4 sec) Excessive workers (8 workers engaged) Process redundancy. (Non Value added processes) Wastages. (Wastage of Time, Material, Man hours and Material) Efficiency was around 51%
  • 21. Before KAIZEN 5 2 3 4 6 8 7 1 8 workers were involved in the production of Rear Combination Light.
  • 22.
  • 23. Tact time is the exact time required to process one product Tact Time = Monthly Operating Time Monthly Production Quantity Old Takt time= 184/3600 hours/piece Old Takt time= (184/3600)x3600= 184 sec/piece New Takt time= 184/5108 hours/piece New Takt time= (184/5108)x3600= 130 sec/piece
  • 24. The graph is showing the Adhesive cleaning as a bottleneck process. The Idle time was very high for several processes for example Idle time for Taping process was up to 89.33%. The efficiency of the processes was 51%. sum of working hours of each process Balance Efficiency = x100 maximum time of process x the number of processes =51%
  • 25. ECRS study was carried out in order to reduce the non value added processes and to eliminate the redundancy. E- Eliminate C-Combine R-Re arrange S-Simplify
  • 26. Previously a non value added process Taping was followed which had no impact on the Product. Taping applied The taping was done to prevent the flowing of adhesive from the back of reflector. After bonding, It was removed.
  • 27. Bulbs were verified at Final Inspection after complete assembly. The process is now eliminated and the bulbs are verified at the time of fitment. Bulb verification
  • 28. Previously two different workers were performing the processes of Inspection and Packing. The packing of parts is done by the inspector at Final Check point.
  • 29. Previously two different workers were performing the operations of Bulb, harness and screw fitment. The processes of Bulb, harness and screw fitment are now combined in a single process.
  • 30. The process of Taping was removed by Gasket fitment. Formerly, taping was applied which was then removed having no impact on the product. The processes are now re arranged by putting the process of Gasket fitment at the first place instead of taping.
  • 31. The testing unit is now simplified and is made common for both the lights. Previously the testing unit for Rear combination had two different units for Left and Right hand lights.
  • 32. Previously the worker had to put the light in press fitment and then had to locate the upper jig. Upper part Lower part Now a jig is developed for Press fitment. New Jig
  • 33. Screw gun was previously placed on the table and hence every time the worker had to take the gun and fit the screws.  The Screw gun is hanged near the screw fitment and hence the worker is facilitated.
  • 34. The Gasket fitment process is eased by making a jig for applying adhesive on the Gasket 1 and pasting the Gasket on the Reflector. 2
  • 35. sum of working hours of each process sum of w orking hours of each proces s Balance Effici ency Balance Effici ency = x100 = x100 maximum t ime of process x t he number of proc esses maximum t ime of process x the number of proc esses =51% =85.87%
  • 36. After KAIZEN 2 3 4 5 6 1 Before KAIZEN 5 2 3 4 6 8 7 1
  • 37. Improvement Parameters Before After % 22.6% Total Cycle Time 612.4 sec 474 sec reduction 34.87% Line Balance efficiency 51% 85.87% increase No. of Workers 8 6 25% reduction Cost reduction in terms of 81.6 min/total 47.4 min/total 41.9% workers workers’ time workers reduction Space saving 264 ft² 216ft² 18.2% saving
  • 38. Work Content analysis was done for two different processes in Leakage testing. 2)1) Leakage testing without Air 3)2) Leakage testing with Air.
  • 39.
  • 40. The reflector was cut in order to see the gap between the Lens and the Reflector.
  • 41. The Lens has a window which is shown in the picture. It was recommended to make a inner wall in the Lens to avoid Leakage
  • 42. The time of Press fitment was changed from 45 seconds to 6 seconds in order to ensure that the locks are properly seated. Previous time New time
  • 43. The flashes inside the channel along the leaked area were removed and then adhesive was applied. The purpose was to check whether the flashes were the root cause for leakage or not.
  • 44. After Press fitment, the pieces are placed upside down on the table to ensure proper adhesion of Lens and Reflector. The purpose was to retain the adhesive along the channel and impart a pressure so as to confirm the proper adhesion.
  • 45.
  • 46. Process: Sealing Team: Leader: Suggest: SMEDA-JICA Before (Problem) 1. Possible damage of Hot Melt Nozzle Because it was installed on the After (Improvement) passage 2. Possible part defect caused by Move the Hot Melt Nozzle to inside the process collision (other worker) Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-5-29 Done Productivity (pcs/mth) Progressing Quality, Cost, 5S, Future NO. Safety, Other_PM (machine protect) Reject Reduced time : 0 hrs./month 1
  • 47. Mr. Salim / Mr. Process: Pressing Team: Leader: Suggest: Adnan Before (Problem) After (Improvement) Change the upper and lower die and upper It takes long time to use the press machine. die fix to the moving plate so that worker can use 1. The worker has to hold the upper base plate Both hands for loading and unloading of the in one hand and put the part from second hand. parts. 2. Possibility of damaging the part and also it take long time to perform the operation. *Shorten the operation time. *Makes worker task easier. Date Target (round mark) Status (round mark) Productivity Result Done [Before – After (sec/pcs)] x Production Vol. 2012-6-5 (pcs/mth) Productivity Progressing (37-20)sec/pcs x 3600pcs/month= 61200 Quality, Cost, 5S, Future sec/month NO. Safety, Other(_____________) Reject 2 Reduced time : 17 hrs./month
  • 48. Process: Team: Leader: Suggest: Mr. Salim Before (Problem) After (Improvement) Sealing performed after application of Rearrange the process and eliminate masking tape on every part “Waste of process itself” *Take much time to masking & remove it *Eliminate Waste process (application of “Waste of process itself” masking tap) *Reduce working time *Waste of masking tape *No masking tape required (cost reduction) Before 1.Sealing After 1.Gasket fitment 2.Bonding/Press 2.Bonding/Press fitment fitment Masking 3.Adhesive cleaning 3.Adhesive cleaning tape Remove Tape 4.Leakage test 4.Leakage test 5.Screw/ Bulb & 5.Tightening Harness 6.Gasket fitment fitment 7.Assemble harness 6.Final testing + 8.Final testing Packing 9.Packing Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-6-5 Done Productivity (pcs/mth) Progressing NO. Quality, Cost, 5S, Future (16-0)sec/pcs x 3600pcs/month= 57600sec/month 3 Safety, Other(____Space_________) Reject Reduced time : 16 hrs./month
  • 49. Process: Leakage Testing Team: Leader: Suggest: Mr. Salim Before (Problem) After (Improvement) 1.It takes long time to check the leakage Use low pressure air for check. 2. Possible overlook the water leak Check by bubble Dip into water and check if water goes into *Shorten the checking time. the part *Ensure the leakage inspection. *No water goes into the part (therefore shorten the cleaning time) Low Pressure Air Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-6-10 Done Productivity (pcs/mth) Progressing Quality, Cost, 5S, Future NO. Safety, Other(_____________) 4 Reject Reduced time : hrs./month
  • 50. Leader: Suggest: SMEDA-JICA Process: Gasket Fitment Team: Before (Problem) After (Improvement) 1-It took long time to perform the operation 1. The idea is to develop a jig with embossed same Because the glue stick with the workers hand Profile as of gasket and it has little higher with base and also the gasket stick with card board. so that 2. Make Operator task more difficult. Glue does not stick with base. 2. There will also be location pins as there are holes Available in the gasket. It will make the operator work more easy and lesser time is required. Location Pins Jig base Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-5-29 Done Productivity (pcs/mth) Progressing (100.57-79)sec/pcs x 3600pcs/month= 77652 sec/ Quality, Cost, 5S, Future month NO. 5 Safety, Other(_____________) Reject Reduced time : 21.57 hrs./month
  • 51. Team: Leader: SMEDA-JICA Process: Final Testing Suggest: Before (Problem) After (Improvement) There was no proper place for A holder is attached to save the putting the markers used in time. marking the parts and there fore the worker took time in marking. Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-6-10 Done Productivity (pcs/mth) Progressing Quality, Cost, 5S, Future NO. Safety, Other(_____________) 6 Reject Reduced time : 0 hrs./month
  • 52. Team: Leader: SMEDA-JICA Process: Final Testing Suggest: Before (Problem) After (Improvement) Coupler was fixed in the Jig which was previously not attached Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-6-10 Done Productivity (pcs/mth) Progressing Quality, Cost, 5S, Future NO. Safety, Other(_____________) 7 Reject Reduced time : 0 hrs./month
  • 53. NO. OF IDEAS BEFORE AFTER TARGET OF Total SMEDA SMEDA IMPLEMENTED IMPLEMENTATION Time saved 88.2 12 0 12 7 1 week of August st hours/month
  • 54.
  • 55. Process: Team: Leader: Suggest: Before (Problem) After (Improvement) Excessive length of bolts *It take long time to tighten nuts Date Status (round mark) Productivity Result Target (round mark) 2012-5-29 [Before – After (sec/pcs)] x Production Vol. Productivity Done (pcs/mth) NO. Quality, Cost, 5S, Progressing 0 Safety, Other(_____________) Future Reduced time : hrs./month Reject
  • 56. Process: Team: Leader: Suggest: Before (Problem) After (Improvement) Date Productivity Result Target (round mark) Status (round mark) [Before – After (sec/pcs)] x Production Vol. 2012-5-29 (pcs/mth) Productivity Done Quality, Cost, 5S, Progressing NO. 0 Safety, Other(_____________) Future Reduced time : hrs./month Reject
  • 57. Process: Team: Leader: Suggest: Before (Problem) After (Improvement) Example of Inadequate lightening for Test lightening at Auto Assembly Line *Possible overlook the defects Dedicate Lightening for Test Productivity Result Date Status (round mark) [Before – After (sec/pcs)] x Production Vol. Target (round mark) 2012-5-29 (pcs/mth) Productivity Done NO Quality, Cost, 5S, Progressing . Safety, Other(_____________) Future Reduced time : hrs./month 0 Reject
  • 58. Process: Team: Leader: Suggest: Before (Problem) After (Improvement) This worker is just holding Jig (waste of time) Hold the Jig by Clamp or something Unload lamps one by one (take a long time) Remove the springs one side all then after remove the other side of spring so that unloading time will be shortened Picture or figure Date Status (round mark) Productivity Result Target (round mark) [Before – After (sec/pcs)] x Production Vol. 2012-5-29 (pcs/mth) Productivity Done NO. Quality, Cost, 5S, Progressing Safety, Other(_____________) Future Reduced time : hrs./month 0 Reject
  • 59. Leader: Suggest: SMEDA-JICA Process: Team: Before (Problem) After (Improvement) Material handling should be improved by making the trolleys in order to reduce the risk of damaging. Date Target (round mark) Status (round mark) Productivity Result [Before – After (sec/pcs)] x Production Vol. 2012-5-29 Done Productivity (pcs/mth) Progressing Quality, Cost, 5S, Future NO. 5 Safety, Other(_____________) Reject Reduced time : hrs./month
  • 60. Time saving on Rear comb. Line =(41.9/100)x184 Time saving on Rear comb. Line =77.096 Hrs/month Time saving on Rear comb. Line =925.152 Hrs/year Cost saving on Rear comb. Line by saving time =77.096x43.47 Cost saving on Rear comb. Line by saving time =3352 Rs./month Cost saving on Rear comb. Line by saving time =40224 Rs./year Cost saving by worker reduction =2x8000 Cost saving by worker reduction =16000 Rs/ month. Cost saving by worker reduction =192000 Rs/ year. Total saving = 1,92,000+40,224 Rs./year Total saving per year = 2,32,224 Rs./year
  • 61. Improvement Improvement in Description Before Target Achieved in % Times Reduce to Total Cycle Time 612.4 sec 474 sec 1.29 1/3 22.6% Line Balance efficiency 51% Around 80% 85.87% 34.87% 1.68 No. of Workers 8 4-5 6 25% reduction 1.33 Cost reduction in terms of workers’ 81.6 min/total min/total workers 47.4 min/total time workers workers 41.9 % 1.72 Space saving 264 ft² - 216ft² 18.18% 1.22 2,32,224 0 - - - Total Saving Rs./year
  • 62. Y9f Cultus Head Lamp.  Takt time and Work Content Analysis of Y9f Cultus Head Lamp.  Y9f Cultus Tail Lamp.  Takt time and Work Content Analysis of Y9f Cultus Tail Lamp.
  • 63. Control P. Adh. Applicator 0.85 x 0.5 CNC Spot Gluing Machine 3 Axis 2.1 x 1.27 Press Table-1 1.0 x 0.7 4.0 m 0.75 x 0.9 0.75 x 0.9 Table-2 0.75 x 0.9 Table-3 Table-4 0.75 x 0.9 Light Tester Leak Tester 0.9 x 0.85 0.9 x 0.7 3.6 m
  • 64. Implementation of KAIZEN. Time study on other Assembly lines.

Editor's Notes

  1. Markers, Points Checking Simplification
  2. Space Savings
  3. Space Savings (MAKE A Column For Before & AFTER)